Gary_Ash Posted April 2, 2019 Share Posted April 2, 2019 I needed to remove the clutch release shaft from a 1937 Studebaker President 8 bell housing, discovered that there were two Woodruff keys in the shaft that had to come out to do it. The outside one was a # 8, 5/32" x 3/4" long, the inside one was a #6, 5/32" x 5/8" long. They had been in there for 82 years and did not want to move. The keyways were so deep, there was nothing to grab on to, so I started down the list of "best known methods". 1. Put a screwdriver blade under the outer edge and pry up. Ha! Nothing to engage the almost vertical surface. 2. Tap on the end of the key to drive it up on the other end. Wouldn't budge, just made big divots in the key. 3. Use a punch to tap down on one end and rotate the key up at the other end. Nothing moved and I was starting to mushroom the top surface. Heated the shaft with a torch to expand it. Nope. Heated the key with the torch, squirted on Kroil, repeat, repeat. Nothing moved. 4. Drill a hole down into the key and use a nail or punch to rotate the key. I tried a couple of nail sets, even beat on them at risk of breaking them off. No joy! 5. Tap the drilled hole, insert a screw, and pull. I ran a #36 drill in as far as I dared, ground off the pointy end of a 6-32 tap and got a couple of threads, but the screw eventually pulled out. 6. Grab the exposed part of the key with ViseGrips or side-cutting pliers. No, not happening. 7. The nuclear option: weld a sturdy piece of steel to the top of the key and drive it upward. I had avoided this since I had to drag the welder from the other side of the garage and I didn't really want to weld the key into the shaft, but now I was desperate since I'd already invested 4-5 hours on the keys. I ground a 5/32 wide slot in a scrap piece of 1/8" steel plate, filed the top of the key to clean it, and hit it with the MIG torch. The first attempt didn't get a good bead on the key, so I tried again with the MIG wire in contact with the key when I pulled the trigger. A few shots and it was firmly attached. Tap, tap with the hammer and out came the key. The inner key was tougher to get at as there was only a 1" space for the 5/8" long key. I cut a slot in a piece of 1"x1" angle iron, welded it on, and had a second success. So, after 6 hours of frustration, I finally got the two keys out, drove out the shaft with a brass drift, and it's on to the next part of the project. 5 Link to comment Share on other sites More sharing options...
Grimy Posted April 2, 2019 Share Posted April 2, 2019 Now THAT'S persistence! Great job, and thanks for the techniques. 1 Link to comment Share on other sites More sharing options...
Matt Harwood Posted April 2, 2019 Share Posted April 2, 2019 A man after my own heart. Did you try swearing and throwing tools? I find that sometimes frightens the parts into cooperating. But if that doesn't work, sometimes all you can do is get creative. Nice work! 2 1 Link to comment Share on other sites More sharing options...
joe_padavano Posted April 2, 2019 Share Posted April 2, 2019 I just went through this trying to remove a Woodruff key in a pneumatic sander that I was rebuilding. Fortunately I did not have to resort to the nuclear option, but now that you've suggested it, I've got it filed away for future reference. Thanks for the tip. Link to comment Share on other sites More sharing options...
Restorer32 Posted April 2, 2019 Share Posted April 2, 2019 Things like that are what makes the restoration business so challenging. Bill the customer "Remove Woodruff key... 6 hours @ $55/hr" ? Exactly why I tell our clients they don't really want a minute by minute invoice. 1 Link to comment Share on other sites More sharing options...
Bloo Posted April 2, 2019 Share Posted April 2, 2019 Well... The good news is your keyways are nice and tight. 1 Link to comment Share on other sites More sharing options...
john hess Posted April 2, 2019 Share Posted April 2, 2019 The better news is a whole bunch of us learned some new tricks... This is why I read the forum regularly... John 1 1 Link to comment Share on other sites More sharing options...
wmsue Posted April 2, 2019 Share Posted April 2, 2019 Thanks for giving us the info. Will keep try and remember it for sure. Thanks Bill Link to comment Share on other sites More sharing options...
nickelroadster Posted April 3, 2019 Share Posted April 3, 2019 I have never had to do this but for some reason it sounds familiar. Everything we do on the old cars makes "book time" sound like a fairy tale. Link to comment Share on other sites More sharing options...
Bhigdog Posted April 3, 2019 Share Posted April 3, 2019 You,re welcome in my shop anytime......bob Link to comment Share on other sites More sharing options...
Frank DuVal Posted April 4, 2019 Share Posted April 4, 2019 If you read the "P" (procedure) pages of a collision crash book (flat rate book for collision shops) you will see the times to R&R parts are based on NEW UNDAMAGED vehicles. Just when was the last time we worked on a NEW UNDAMAGED vehicle to fix damaged parts?😲😯😁😵 Great work with the welder!👍 Link to comment Share on other sites More sharing options...
jan arnett (2) Posted April 5, 2019 Share Posted April 5, 2019 where there is a will there is a way and you found the way. Link to comment Share on other sites More sharing options...
R Walling Posted April 10, 2019 Share Posted April 10, 2019 I like the way you cut the slot in the angle iron. There was no way to weld the key to the shaft. Link to comment Share on other sites More sharing options...
chistech Posted April 10, 2019 Share Posted April 10, 2019 (edited) Another way I learned was to put two lengths of tape alongside the key and run a bead of weld down the top of the key. The weld shrinks the key and it will pull out. Works the same when removing inner tapered races that you can’t get behind. A bead of weld around the face and the race falls right out it shrinks so much. With your key being deep in the shaft, your method of straddling the key with sacrificial metal was probably the best way to go. I do have a tig welder which is very, pin point controllable, and it is perfect for the above process when you can’t risk an “oops!” Great Fix. Edited April 10, 2019 by chistech (see edit history) 1 Link to comment Share on other sites More sharing options...
Mark Shaw Posted April 10, 2019 Share Posted April 10, 2019 1 hour ago, chistech said: run a bead of weld down the top of the key. The weld shrinks the key and it will pull out. Works the same when removing inner tapered races that you can’t get behind. A bead of weld around the face and the race falls right out it shrinks so much. I agree; This is how I removed the bearing race in my Shaw DuAll Tractor. It works like magic! Link to comment Share on other sites More sharing options...
MikeC5 Posted April 13, 2019 Share Posted April 13, 2019 These are good tips! Thanks guys. Link to comment Share on other sites More sharing options...
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