avgwarhawk Posted April 13, 2017 Author Share Posted April 13, 2017 3 hours ago, Bill Stoneberg said: Clocks are easy to fix. There are a set of points in it that get corroded. Blow the dust out, oil lightly and clean the points. Chances are it will work again. Bill, I took a quick look a week or so ago. First place of course was looking at the fuse. Trusty test light found power on one side and not the other. But, the fuse inside looked ok. No matter. Went to replace it. As I worked on removing the fuse power was found through the fuse and clock was working. Of course humans being humans we adjust our clocks to the correct time. It was at this juncture the clock stopped again. I did not recheck the fuse at that time. I had a laundry list of items to tend to. I will tackle the fuse once again. If it test good the clock will come out for a clean and oiling. Thanks for the tip! Link to comment Share on other sites More sharing options...
avgwarhawk Posted April 13, 2017 Author Share Posted April 13, 2017 1 hour ago, Beemon said: Don't use a point file, use a burnishing tool like emery cloth if cleaning the points up. Thanks for the tip! Link to comment Share on other sites More sharing options...
avgwarhawk Posted April 16, 2017 Author Share Posted April 16, 2017 New set of Coker 2 1/2 WW bias ply on the rear installed this weekend. There is no doubt the US Royals have been on the Buick for quite some time. Repacked the front wheel bearings. I like a bit more bearing grease then what was there. Inspected all brake components. All return springs, cylinders, hard lines, shoes and master have less than 600 miles on them. Good to go. Wrap this up with a new fuel pump and carb rebuild. Look into the heater core/valve at the end of summer. 1 Link to comment Share on other sites More sharing options...
Bill Stoneberg Posted April 17, 2017 Share Posted April 17, 2017 Did you check your brake lines too ? I ask as I found a bubble in mine. 1 Link to comment Share on other sites More sharing options...
JohnD1956 Posted April 18, 2017 Share Posted April 18, 2017 On 4/16/2017 at 1:59 PM, avgwarhawk said: Look into the heater core/valve at the end of summer. Actually, that leak could cost you significant temperature issues during the summer. Are you going to by-pass the heater altogether for now? 1 Link to comment Share on other sites More sharing options...
avgwarhawk Posted April 18, 2017 Author Share Posted April 18, 2017 15 hours ago, Bill Stoneberg said: Did you check your brake lines too ? I ask as I found a bubble in mine. The entire brake system has been replaced. All rubber hoses, metal lines, master cylinder, wheel cylinders, return springs and shoes. I have pulled and inspected all drums. No leaking in the rear wheel seals. New seals on the drums up front. She stop very well for 2 tons of vehicle. 2 Link to comment Share on other sites More sharing options...
avgwarhawk Posted April 18, 2017 Author Share Posted April 18, 2017 12 hours ago, JohnD1956 said: Actually, that leak could cost you significant temperature issues during the summer. Are you going to by-pass the heater altogether for now? The cooling systems does keep pressure when running at operating temperature. My diagnosis as a result of pressure in the system while hot is the control valve is working and a leak at the core when valve is open. What is odd is when the heat is first switched I get the faint smell of antifreeze. It dissipates very quickly and no issue after that. I drove the Buick about 60 miles in 80+ degree weather this past weekend. No over hearting. At any rate, I will leave it as it stands for now and pull down the heating box at the end of the summer. Link to comment Share on other sites More sharing options...
avgwarhawk Posted April 18, 2017 Author Share Posted April 18, 2017 New fuel pump on. The rubber fuel hose from pump to the hard line was on the way out. One stiff tug and it came apart. The hard fuel line was in great shape. The hose clamp at the hard line connection at the frame is a unique design. It has a hook type design that hooks to the clamp to the frame so if the rubber line was pulled for whatever reason the hook on the clamp would keep the rubber line from pulling off the hard line. I guess it would be prudent to check the rubber hose in the tank area. 3 Link to comment Share on other sites More sharing options...
avgwarhawk Posted April 21, 2017 Author Share Posted April 21, 2017 Spending time with the 60. Clock is running like a well oiled watch. Ummmmm......it's running. 3 Link to comment Share on other sites More sharing options...
Guest LeCat Posted May 7, 2017 Share Posted May 7, 2017 (edited) On 2017-04-21 at 2:57 AM, avgwarhawk said: Spending time with the 60. Clock is running like a well oiled watch. Ummmmm......it's running. Hmm. Mine has stopped at 5 to 4, need to take a look at that..... some day. Awsome looking clock that deserves to work like... a clock Edited May 11, 2017 by LeCat (see edit history) Link to comment Share on other sites More sharing options...
avgwarhawk Posted June 12, 2017 Author Share Posted June 12, 2017 It was time to pull the carburetor for a rebuild. Hesitation and flat spots. I found the channel under the carburetor loaded with carbon flaky powdery nastiness. It was good and clogged. Removed that bit of nasty crap. The entire carburetor was well covered by years of gook and grime. Other than the clogged passages under the carb the La Brea Tar Pits sludge covering the carb as well as inside the carb was cleaned out. After inspecting when the cleaning as done I made the decision to reinstall and see what she runs like. The engine idles fine. Performance as fine. Just that annoying hesitation and flat spot that would rear it's ugly head when it felt like it. Further, the accelerator pump squirted gas as design. So, call me crazy or call me a tow truck I reinstalled. Much to my surprise the carburetor performed flawlessly. So screw it. I drove on.... 3 Link to comment Share on other sites More sharing options...
Pilgrim65 Posted June 12, 2017 Share Posted June 12, 2017 Interesting tips re clock , will see if works on my 53 cheers pilgrim Link to comment Share on other sites More sharing options...
Smartin Posted June 12, 2017 Share Posted June 12, 2017 Those rochesters are infamous for the bog. I have given up on several of them and just dealt with it. Link to comment Share on other sites More sharing options...
avgwarhawk Posted June 13, 2017 Author Share Posted June 13, 2017 3 hours ago, Smartin said: Those rochesters are infamous for the bog. I have given up on several of them and just dealt with it. She was bogging quite a bit. Feather the pedal when accelerating from a stoplight. Bog when accelerating at speed. After clean up the bog is just about nonexistent. Much improved and more positive/responsive when pressing the gas pedal. When the secondary open she really moves. I'm pleased with the results. 1 Link to comment Share on other sites More sharing options...
dei Posted June 13, 2017 Share Posted June 13, 2017 On 2017-4-12 at 6:17 PM, avgwarhawk said: I feel like Johnny Cash. One piece at a time. Out with the old and in with the new.. Just a question / comment. When I had my car up on the hoist and my mechanic looked at these, he said that they were installed upside down. It has a long time ago when they were replaced and can't remember if I did them or the mechanic at that time did them. His rational was that if you went over something a bit high those threads would catch and either bend them or break off.... Have you noticed how they are on any other of your cars? My other cars are not handy close by to look and besides, it's not the getting down to look that comes into play, it's the getting back up. Link to comment Share on other sites More sharing options...
avgwarhawk Posted June 13, 2017 Author Share Posted June 13, 2017 (edited) 4 hours ago, dei said: Just a question / comment. When I had my car up on the hoist and my mechanic looked at these, he said that they were installed upside down. It has a long time ago when they were replaced and can't remember if I did them or the mechanic at that time did them. His rational was that if you went over something a bit high those threads would catch and either bend them or break off.... Have you noticed how they are on any other of your cars? My other cars are not handy close by to look and besides, it's not the getting down to look that comes into play, it's the getting back up. My 60 is unmolested. The original link kits that I removed where installed just as you see the new link kits in the pictures. Also, at the top of the link kit, if the threaded portion was in that position when installed it could possibly rub the frame. Edited June 13, 2017 by avgwarhawk (see edit history) 1 Link to comment Share on other sites More sharing options...
old-tank Posted June 13, 2017 Share Posted June 13, 2017 8 hours ago, dei said: it's not the getting down to look that comes into play, it's the getting back up. Time to get back down anyway. The rubber grommets are not compressed enough. Those links are to be installed until the nut bottoms on the rod threads On some replacements new threads may need to be cut. Link to comment Share on other sites More sharing options...
avgwarhawk Posted June 13, 2017 Author Share Posted June 13, 2017 22 minutes ago, old-tank said: On some replacements new threads may need to be cut. And there is this. Link to comment Share on other sites More sharing options...
kgreen Posted June 13, 2017 Share Posted June 13, 2017 On 4/8/2017 at 11:08 PM, avgwarhawk said: The ride height remained the same. She sits level. The rear with no one in the back seat would bottom out/hit the rubber bumpers with the old springs. Some sagging. I have always done well with the progressive coils. The ride is the same as the old coils. A bit less body roll. The front coils are fine and will remain. Shocks will be replaced. What's the theory behind progressive springs? I'm guessing that the first several hundred pounds is carried by the light weight end of the spring and as the weight increases, the lightweight end is nearly fully compressed and the heavy weight end of the spring takes over. In other words, the soft ride first progressing to more firmness as the weigh increases. Am I close? 1 Link to comment Share on other sites More sharing options...
avgwarhawk Posted June 14, 2017 Author Share Posted June 14, 2017 21 hours ago, kgreen said: What's the theory behind progressive springs? I'm guessing that the first several hundred pounds is carried by the light weight end of the spring and as the weight increases, the lightweight end is nearly fully compressed and the heavy weight end of the spring takes over. In other words, the soft ride first progressing to more firmness as the weigh increases. Am I close? Yes! 1 Link to comment Share on other sites More sharing options...
avgwarhawk Posted September 16, 2017 Author Share Posted September 16, 2017 Had a hearter core leaking issue. Not a large leak but some fog on the windows in cool weather and smell of antifreeze. I pulled the heater core assemble. When taking the assembly apart I found that the assembly had been removed at one time as the tell tale signs were evident. The core was found to be in good shape. It appears the control valve was leaking some. Upon removing the control valve...which should take no less than 30 seconds was a bit more for me. The one stud of the three spun as the nut was turned for removal. Dremel tool to the rescue. The core had quite a bit of scale. I used a dilute potion of muriatic acid and water. Passages free flowed much batter after a short sit of a few minutes. I rinsed and rinsed to assure the acid was gone and then added a solution of baking soda. Rinsed and repeated with the rinse. The next task was locating a valve ready to go or send in my valve plus $$$$$$$ to have it repaired. Good old Harrison: I was able to find a Harrison for a 60 Chevy. It is one and the same with exception of the replacement had the smaller diameter tube and I had to move my copper thermal coil to the replacement. I cut my own gasket for the valve as well as a gasket for the area between the firewall and core assembly. Once assembled it made sense to me to hook up the valve/core assemble and let the 401 fill it with hot water/antifreeze and check for leaks. I don't have a radiator pressure tester. It was found to be leak free, got hot and ready for install after my test. Reassembly took about 45 minutes. Job done. 1 Link to comment Share on other sites More sharing options...
KongaMan Posted September 16, 2017 Share Posted September 16, 2017 (edited) 1 hour ago, avgwarhawk said: I don't have a radiator pressure tester. You can fashion one from a couple of pieces of heater hose and a tee: - Connect one end of each piece of hose to the core. - Connect the other end of each piece of hose to the tee. - Submerge the core, then stick the tip of an air nozzle into the tee, pressurize, and look for bubbles. If you want to go a step further, you can put a schrader valve on the tee so you can pump it up once and do a leak-down test. Edited September 16, 2017 by KongaMan (see edit history) 1 Link to comment Share on other sites More sharing options...
avgwarhawk Posted September 17, 2017 Author Share Posted September 17, 2017 I thought about using air. It was easier to hook to the core and test. Link to comment Share on other sites More sharing options...
avgwarhawk Posted February 25, 2018 Author Share Posted February 25, 2018 The well known corroded headlight switch/ dash lights rheostat. Did not bother to clean it up. It was out in 5 minutes. Replaced same. 4 Link to comment Share on other sites More sharing options...
avgwarhawk Posted April 25, 2018 Author Share Posted April 25, 2018 I guess there was no aftermarket replacement or they did not look for one. Although it worked, getting a new aftermarket rear parking brake cable is the wise thing to do. Don't try this at home. 3 Link to comment Share on other sites More sharing options...
Beemon Posted April 25, 2018 Share Posted April 25, 2018 I would put one or two more in line just as a back up. There's a lot of force in the cable when you ratchet it down with the parking brake peddle. Link to comment Share on other sites More sharing options...
avgwarhawk Posted April 25, 2018 Author Share Posted April 25, 2018 2 hours ago, Beemon said: I would put one or two more in line just as a back up. There's a lot of force in the cable when you ratchet it down with the parking brake peddle. No need. There are new direct replacement cable available. This device was installed by the previous owner. Took no time at all to remove and replace. Fortunately the front cable to the pedal is not overstretched. It's even more fortunate new parts like this are available. 3 Link to comment Share on other sites More sharing options...
avgwarhawk Posted May 4, 2018 Author Share Posted May 4, 2018 Neat find here. Picture of the previous owners grandfather and aunts. The 60 in the background: Here she is today: 5 Link to comment Share on other sites More sharing options...
avgwarhawk Posted May 19, 2018 Author Share Posted May 19, 2018 Finally got to the wing window crank issue. It is raining cats and dogs here in MD so what a better time then to dig into a window crank issue right? Right!! When I purchased the 60 the crank was in the glove box. Owner said he could got get it to stay in place. Investigating the shaft in the door, it had pushed through for some reason. I disassembled the door card to get at the inner workings of the door. Fairly simple with correct tools to disengage the small pins that hold the outer edge of the door card secure. Just a few. The rest are screws. Proper tool to disengage the large window crank handle is always a plus. Upon investigating the issue, the shaft that the crank is secured simply pushed through the housing and was found inside at the bottom of the door. As I fiddled and searched I found other odds and ends to the gear mechanism that operates the wing window. Fished out a backing plate, washer and spring type washer. No idea how it fell apart....not until I slipped in the shaft with worm gear. As I cranked it slowly backs itself out. So, what holds it in place? The nice backing plate found in the bottom of the door of course. Question is, how is the plate secured so the worm gear does not work it's way out? No screws found in the door with the other pieces of the mechanism. I had to remove the entire assemble. Easy enough. One bolt that holds the glass frame to the housing. Three screws that secure the housing to the door. Here are the puzzle pieces: I found the grease inside was stiff as a board. More than likely the cause for allowing the gear to push it's way out deforming the pressed metal that holds the back plate in place. I discovered this after a few attempts. I cleaned off the old hardened grease. Applied new lube and the entire mechanism cooperated much better. Pictured here is the securing forms for the backing plate that hold the worm gear in the housing. I assemble the mechanism with the washer at the end of the worm gear inside the housing. The spring type washer at the front of the housing. The two towers of metal that hold the plate in place I simply used a punch and hammer(lightly) to deform it and compress the plate to the housing. It is not beautiful and does not need to be. It only needs to hold the plate in place so the worm gear does not worm it's way out. Reassembled the door card. Window crank went in without issue. Wing window is now open for business. 5 1 Link to comment Share on other sites More sharing options...
EmTee Posted May 19, 2018 Share Posted May 19, 2018 12 hours ago, avgwarhawk said: I simply used a punch and hammer(lightly) to deform it and compress the plate to the housing. That's it -- the plate was riveted (actually swedged) on, using the posts cast onto the housing. The posts must either have originally not been flattened enough, or maybe too much (leaving the 'head' too thin). Good fix! Link to comment Share on other sites More sharing options...
old-tank Posted May 19, 2018 Share Posted May 19, 2018 On some of my 55's there was not enough material to swedge back over. So I drilled and tapped for a screw. 1 Link to comment Share on other sites More sharing options...
avgwarhawk Posted May 19, 2018 Author Share Posted May 19, 2018 5 hours ago, EmTee said: That's it -- the plate was riveted (actually swedged) on, using the posts cast onto the housing. The posts must either have originally not been flattened enough, or maybe too much (leaving the 'head' too thin). Good fix! Quite possibly flattened enough but the hardened grease and worm gear action it found the path of least resistance. That path was pushing the plate off. Then again the posts had little to no deformity from swedging. I took care of that with a hammer. Link to comment Share on other sites More sharing options...
avgwarhawk Posted May 19, 2018 Author Share Posted May 19, 2018 4 hours ago, old-tank said: On some of my 55's there was not enough material to swedge back over. So I drilled and tapped for a screw. That was my next trick up my sleeve. After new grease, the worm gear wanting to push out the back plate instead of turning the window stopped. If it fails again I'll use screws. 3 Link to comment Share on other sites More sharing options...
Beemon Posted May 20, 2018 Share Posted May 20, 2018 Thanks for this explanation. I've always wondered why my wing window cranks always screwed into the door card until I pulled out both wing windows recently and discovered there weren't any backing plates. Assuming 56 is similar to 60, now I know what to look for and what to do! 1 Link to comment Share on other sites More sharing options...
avgwarhawk Posted May 20, 2018 Author Share Posted May 20, 2018 (edited) 21 minutes ago, Beemon said: Thanks for this explanation. I've always wondered why my wing window cranks always screwed into the door card until I pulled out both wing windows recently and discovered there weren't any backing plates. Assuming 56 is similar to 60, now I know what to look for and what to do! Will said the 55 are similar. Yours should be as well. Let us know what you find with yours. Edited May 20, 2018 by avgwarhawk (see edit history) Link to comment Share on other sites More sharing options...
avgwarhawk Posted December 5, 2022 Author Share Posted December 5, 2022 (edited) And there is more to the story!!!! The previous owner's son was able to dig up the information on the original owner of this 1960 Electra. Tom had relayed the history of the Buick and the low mileage was due to a band member owning the Buick but never drove it much. The Buick was purchased and owned by a band member in the local Altoona/Tyrone PA area. Tom's grandfather was friends with a gentleman named Glen Waring who was a brother to Fred Waring. Fred Waring is the band owner and leader! Fred Waring and the Pennsylvanians. Fred wanted to sell the Buick because he was never in town to drive it. Thus the low miles(19000) when purchased(1976) by the second owner(Tom's grandfather). Tom's grandfather did not need a car but it was a bargain. He parked the car in the garage at his local business until 2001. It was eventually passed to his son who passed several years ago. And then sold into my care. Original owner Fred Waring His band. Fred Waring and the Pennsylvanians. Other info on the band. See link. https://en.wikipedia.org/wiki/Fred_Waring Waring Shawnee Inn Delaware PA: Edited December 5, 2022 by avgwarhawk (see edit history) 5 1 Link to comment Share on other sites More sharing options...
Recommended Posts
Create an account or sign in to comment
You need to be a member in order to leave a comment
Create an account
Sign up for a new account in our community. It's easy!
Register a new accountSign in
Already have an account? Sign in here.
Sign In Now