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junkyardjeff

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Posts posted by junkyardjeff

  1. I have a 68 Electra in the shop for a interior and while waiting on materials I started tinkering with the glove box lock that fell apart on the owner,the lock cylinder comes out first and then there is a retaining nut kind of built in the dash that holds on the rest and it takes a special tool. It looked like it was a 1/2 allen but no its not so I posted in the Buick section hoping someone with a 68 B body shop manual can get me the part number for that tool if its mentioned in it.

  2.  There were at least 4 shops in town that installed those seat covers many years ago and some with in a few blocks of each other,two of those shops are still in business and I worked at those two over the last 30 years. One shop still had rolls of that type material that was never used during the 14 years I worked there and a few years after I quit I went back and he threw them out.

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  3. I always thought those older motors were the best but even though the later motors did not have the power they were able to go more miles before repair,I am a little dissapaointed those heads did not get to 50,000 before wearing out. When it goes back togather I will take the 190 degree thermostat out of it,I was chasing down a lack of heat issue from the heater which turned out to be a bad heater core and never removed it so i had been running it a little hot.

  4. Got some bad news from the machine shop,those heads that only have 48,000 miles are worn out and need all new intake valves and guides plus the one exhaust valve and will be around 500 dollars to repair. He told me all the motors of this era were like that and I was told by others it was common to for that era of motors to need a valve job around 50,000 so I am going to pick up a later set of heads to have gone through. I have put over 200,000 on the late 80s and up 302s without any valve problems so its going to get a set of E7 heads.

  5. I installed a 16,000 original mile 302 in my 65 custom 500 10 years ago and have since put 32,000 miles on it and burnt a exhaust valve last sunday,I was going to blame it on the crappy gas we have today but after I tore the motor apart I think I might have found the problem. 8 years ago I changed it over to a 4 bbl since I had to pull the intake to replace what I thought was a bad lifter that was making noise after the 30 storage of the motor,instead of buying a good name brand of intake gasket I ordered a installation kit with the intake and the gaskets are too big around the intake ports and the gaskets were haging a little too low and not much to seal on the bottom of the ports so I think it was running a little lean and also using oil that it did not do until the intake change.post-83995-0-11945100-1449946228_thumb.jpost-83995-0-07765400-1449946254_thumb.j

  6. That motor is definately tired,plenty of smoke out the tail pipe and road draft tube and the oil cap. We did not check the point gap but the timing was retarded about a 3/4 inch away from the mark,I wish I could have been more helpfull but its rebuild time for that 223. I drove my 65 custom 500 down there and burnt a exhaust valve on the trip so it looks like I have some work to do too.

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