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1964 Austin Healey Sprite - Bugeye


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British tube fittings are unique to British cars. But the tube itself is standard imperial tube. I almost always make my own lines, re use the fittings . I have lots of spares off parts cars if the fitting is damaged. But note the flares are different from regular U.S. practice flares. They are usually called  " bubble flares ". and they can be a bit tricky to form. Also note the fittings themselves can become distorted if they are tightened too hard. The part of the fitting closest to the flare can itself become flared out and becomes very hard to start back into a new component. If the distortion is minor you can file them back to the correct shape. If they are badly opened up it is best to replace them. New ones , both the fittings themselves and pre made lines ,were at one time readily available . But these days you probably have to order from Moss. Keep a new fitting on hand as a guide for reference as to the re usability of your old fittings and a guide to how it should look after you repair old distorted fittings.

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Thanks - I'll see what happens with the tube I installed, because the thread on this replacement slave cylinder is not the same as what was on the car (and I got this cylinder from Moss). The fitting that came off the car - I'll try to clean that up for possible future use, but it was pretty corroded.

 

I tried to bleed the system yesterday, but the fluid couldn't make it "over the hump". Checking the AH forum, this seems to be very common, so I ordered the pressure bleeder recommended there. (Gunson Eezibleed, ships from UK) The "hump" is the fact that both lines exit the top of the master cylinder, go up the firewall a couple of inches, before routing across the firewall and back down on the right side. More widely available (and universal) vacuum bleeders seemed to not be as reliable for this system.

 

On one side, it seems strange to me that a master cylinder whose job is to pump fluid can't pump it upwards a little, but it may really be the weight of the fluid in the upward-routed tube that falls back down into the cylinder even with the bleed closed on the outlet end, so the fluid never makes it up and over to where an equal amount of downward-running fluid would be present to counterweight the upward-running fluid.

 

While I wait for that bleeder, I'll see what else can get done.

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10mm and 3/8 inch are very close so if trying to identify the threads be very careful. For example, if you have a slave cylinder that takes a 10mm fine thread and go to put a 3/8 fine thread in it it may "seem" to fit. It may even seem to be correct. 8 mm and 5/16 in are similar I think.

My car happens to require a bubble flare at the brake master cylinder, but then a regular flare at the downstream fitting. I think I made the mistake of using a 3/8 fitting in something that should have had 10 mm once.

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It seems strange that the new cylinder is a different thread. Did Moss advise you this is the case ? Some of the very late versions of the sports cars did change to updated threads. For example a late Triumph Spitfire MC is often used on Lotus Europa's from the later 1960's and early 1970's. It is a lower cost interchange with the O.E.M. master. Except the fittings are different so either the fitting must be changed or an adapter fitted.

 But I would be surprised you would run into this unless you tried to use the dual circuit master from a very late Midget.

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Yes, if it's the difference between 10mm and 3/8" with the exact same pitch - this seems unlikely though, because if it's a 20 thread / inch pitch, I'd expect a similar metric-pitched thread to not exactly match that and bind up at some point. When I put the original fitting into this new cylinder, it does just that - diameter is very similar, but pitch binds it up in a turn or less.

 

Anyway, I doubt that Moss knows exactly what they're selling. Many of their items are UK sourced, but some are not. I just looked, and I must have already thrown out the box that this slave cylinder came in, but the box for the master says "Made in China", so I don't have great confidence that all features were necessarily specified exactly the same in the reproduction part. I won't know if it leaks until I try the pressure bleeder (maybe in about a month from now, depending on how shipping goes). If it doesn't leak, then great. If it does, I'll work options from there. Fortunately there is a British specialist repair / restoration shop not far from here, so I could work with them to get this tube made up and replaced. I want to minimize their assistance, though, because their rate is just over $100/hr.

 

For comparison, I paid under $3 for the tube that's in there now, and I wouldn't be surprised if their help was at least $100. If this becomes the difference between car is drive-able or not, I'll pay for good help, but this also motivates me to do as much as I can on my own. 

 

Our weather has finally turned to winter, so I'm not motivated to go out in the garage and do anything. I know, this is nothing compared with what a lot of others have to work with. It hasn't even frozen here yet, but that's forecast for over this weekend.

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Did some digging on the ahexp.com site, and the slave pressure line thread is supposedly 3/8 - 24, so I don't know what came off of the car, but it's not that. If the change to the front bodywork is any indication, this car has had some things changed around, so I'm not surprised the slave cylinder may have been from another year, model, or a totally different car that just happened to fit.

 

Weather cleared up, so I got the differential oil changed. This also included thoroughly cleaning the drain & fill plugs - still a messy job, but maybe not quite so messy on reinstalling the cleaned-up plugs.

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Pretty light first week back at work, so I took off early and got the starter swapped out. This proved to be a good call. The starter that was on there would turn intermittently, and I don't know what would put it into the right position to turn. A reman starter was about $35 with shipping (when I get the core charge back), and it definitely has good power. Spun it for a couple of seconds, and I could hear the sound change as the oil pressure came up on the gauge, so that's good. I also swapped out the distributor cap and leads while in that area.

 

Found clear steps on the ahexp.com site - remove ignition leads and distributor cap, pull out distributor, loosen top starter bolt, remove starter cable from starter, remove nut from bottom starter bolt, go back up top, finish removing upper starter bolt, pull starter out from top. Installation is reverse of all that - pretty easy.

 

Coil might be bad. I'll check on how to check it.

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Looking good ! I have very fond memories of the Bug Eye's / early sliding window Sprites and Midgets of my youth. I have been looking for another one for a few years now, but they seem to have dried up in my area. At one time they were almost as common as VW beetles. I still have a good quantity of mechanical parts stored away , more for my wife's Morris Minor convert and my Buckler basket case. But eventually one will turn up. There was one back in the summer  { rough but intact $500.00 project car }, well out of my area . About a days drive into the British Columbia interior. By the time I mulled over whether it was worth two days of driving  someone else snapped it up.

Edited by 1912Staver (see edit history)
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Replacement coil showed up - another sign of the times, it was showing as "delayed" for the past 2 days. No big deal - it arrived. So this led me to pull off the old coil, which I should have done while waiting, because the bracket needed a clean-up. Couple of minutes in the blaster and the bracket's good - looks like it didn't have paint originally. The bolt will sit in the Evap-o-rust overnight. I put the coil in without the bracket and checked for spark - no good. Anyway, the coil I pulled out had a date code from 1973, and the car's been in storage 20+ years, so ~$15 for a new coil isn't a big deal at all. I also have a points & condenser set to install. The Gunson Eezibleed showed up today - actually ahead of promise date from the UK.

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Edited by Eric W
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Did a little more disassembly not directly related to getting things going. Pulled out the heater fan & heater core. Pulled out the right side footwell cover plate. One of the fasteners was rusted to the point that the 7/16" wrench couldn't get a bite, so I cut a slot in the head for a screwdriver. That wasn't working, so I hit it with the torch for a few seconds. It lifted right out. I'll clean up the cover plate so things on that side look better, and come up with a heater block-off plate. I can add the heater back if/when needed.

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Not such a good day today. I'm working in a fairly over-packed garage that only has 2 power outlets. One is on the other side of the garage behind a refrigerator. So the one I can get to is usually for a radio and light somewhere. So when using the media blaster, I plug in the light inside the blaster, and run an extension cord from near the front door of the house to the air compressor, then run the air hose to the blaster. So I got that set up this morning, heard the compressor kick on, then I was headed into the house for something. I came back out, went over to the blaster, and started the cover panel pictured above. Usually, the compressor kicks on almost instantly (it's a fairly small one), but it didn't kick on. Then I felt the pressure going down. Checked on the compressor and it's dead. So I did a little searching and I think it's the pressure switch that cuts the power on & off. Ordered another one of those.

 

Then I moved on to getting the coil into the cleaned up bracket. The new coil is just the slightest bit larger diameter than the old one, so it was a battle to tweak the bracket's shape until the coil fit and the securing bolt also fit at the same time.

 

Then I decided to move on to trying the Gunson Eezibleed. It's set up to replenish the fluid in the master, but one of the comments on the ahexp forum was to run the replenish bottle with only air, so it's just putting air pressure directly into the master. So that's how I ran it - as an air pressure adder only. Its air supply is a Schrader valve adapter to go onto a tire. I checked the tire pressure because it says to run the bleeder at 20psi or less - the tire was at 40psi. So I bled that down to 20. Got set up to bleed the right rear. Went through nearly every wrench to find that the rear bleeds are 9/32". Connected the bleeder to the master cylinder, then to the tire, then opened the bleed on the wheel cylinder. It pushed fluid through no problems. Close the bleed, disconnect bleeder from the tire, set up bleed on the left rear. Checked fluid level in the master, added fluid. Reconnected the bleeder to the master, then to the tire for pressure, bled the left rear. Then noticed drips below both front calipers. These are banjo fittings with a pair of copper crush washers. So I tightened those and set up to bleed the left front. Topped up the master again. Front bleeds needed 3/8" wrench. Bled left front, topped up master, then right front. Saw drips again at both front calipers, so tightened the banjo fittings a little more. Checked the pedal, and it didn't feel good. Checked the brake line at the master, and it's weeping there. Tried to tighten that fitting (on the back side of the master, buried in the pedal box, so you can't see it). This is probably the thing that will make me remove the front sheetmetal, because that brake line fitting is impossible to see and touch at the same time with the hood on.

 

This goes back to the over-crowded garage - I don't have anywhere to go with the front sheetmetal if I pull it. I've seen others stand it up on the back edge - that's a vertical seam on the body, so maybe I can stand it up.

 

Tried to bleed the clutch the same way (it's a single fluid reservoir for both the brakes & clutch). The first tire was down to almost no pressure, so bled another one down from 40 to 20, reconnected everything, but no fluid came out of the clutch bleed. Not sure what's going on there. Line may be blocked or pinched somewhere.

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  • 2 weeks later...

Between being sick this week and trying to cover work as much as possible, I didn't get much done at all in the garage. Finally did get out for a fitting to put the new pressure switch on the compressor. Got that put on and nothing. Decided to look online for the instruction manual (I have an idea where I might have stashed the paper copy, but online search is very quick.) There it is, buried between the motor & the tank, a breaker for the the motor! Reset that, and compressor going again. Oh well, <$20 for the switch & fitting.

 

Blasted and painted the passenger footwell cover plate. Watched a video about forming bubble flares on brake lines. Doesn't look too hard - just need the right die (which I don't have). In the interest of continuing to do what I can, I'll probably get a die set and take a shot at re-making the clutch and brake lines. Clutch line acts like it's blocked, and the brake line is leaking at the master.

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Pulled out the clutch and brake lines. Clutch line looks good. I think it didn't bleed correctly due to the leak of the brake line at the master cylinder. After pulling the brake line, I could see that the bubble flare is cracked at the master cylinder end, so that would explain the leak. I've been researching replacement lines. From the AHEXP forum, they mention Fed Hill as a source (U.S. distributor for UK-made fittings and lines). Those posts were 9+ years old, but Fed Hill is still around and has fittings available, though it's quite possible that the fittings on the existing tubes could work, because all they do is hold the bubble flare in place. I may take a shot at re-using the fittings with a bubble-flared 3/16" tube from the FLAPS, and if that doesn't work, then order new from Fed Hill. The brake line is ~63.5" long

 

Couple of photos of the line routing, though I got the old lines out in good shape for patterns.

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Re-bled the brakes and the pedal feels good! Now the clutch won't bleed at all. I'll go over that line again. Maybe I'll feel motivated to do something with it tomorrow.

 

...

 

Later - I suctioned fluid out of the clutch side of the master cylinder and pulled the clutch line. Formed a new line section at the master from the segment left over from the brake line. Transferred the original line fitting to the new tube with the bubble flare. Should work better now.

 

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Edited by Eric W
clarification, added photos (see edit history)
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  • 2 weeks later...

Last couple of days - called Moss tech support about the master cylinder. They've agreed to a return / replace, so I need to get it back out. Took it out, moved the clutch side with a screwdriver (where the pedal pushrod goes), and fluid comes out the clutch port. So I put it all back in and tried again. Still no luck, so I think the cylinder may be leaky / not pushing with full power or something. I did adjust the clutch pedal pushrod to be longer, to be sure the pedal was getting a full stroke on the piston in the master cylinder, but still no results.

 

Read numerous websites about bleeding these clutches. Seems people try every which way to get these done - one that I might try was to run a hose from the right front brake bleeder to the clutch bleed, then pump the brakes to back-fill the clutch. The clutch and brake reservoirs are common at the master, so fluid just circulates around (don't need a hose or something between the clutch and brake reservoirs).

 

Another one that was kind of interesting is to get a piece of hose that fits over the master cylinder fill port threads and a worm clamp to make the hose tight on those threads, then flood the master cylinder to a level up in the hose that is higher than the clutch hard line. Then gravity should move fluid up and "over the hump" in the line down to the slave cylinder.

 

I'll get that cylinder out today & maybe get to a shipping place to get it on the way back to them.

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I did try the piece of hose over the master fill port (gravity bleed) before giving up on this master cylinder. Though before doing this, I swapped out the lower segment of clutch hose because I had made that with not the bubble flare, though it did seem to be leak tight (with no pressure). I had a piece with preformed bubble flares so swapped that in. Wouldn't want to go through all this to get the clutch bled just for it to leak.

 

Got 7/8" ID rubber hose, cut about 8"-9" long. It pushed right onto the master fill port. I put a worm clamp around it just to put a little compression on the rubber so it wouldn't leak. Filled this up near to the top. Waited a while - no level change. Pumped the pedal many times - no level change. Realized the clutch side of the cylinder is leaking where the pedal pushrod goes in - that could be a problem. So I suctioned out the hose as best I could, removed the hose and got the master cylinder out, drained, wrapped up and packed for return.

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While the master cylinder is out, I decided to see if I could get spark. Pulled the distributor, swapped out the condenser, and cleaned the points. Put the distributor back in. Checked that the coil is getting power, then engaged the starter switch (no solenoid, just a cable-actuated mechanical switch above the starter). Had the #1 plug out and held against the engine for ground. Saw a spark on the fuse block, but no spark at the plug. The spark I saw was a fuse. I'll check the diagram to see what that's for.

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Got it started! Ok, I can get it driving from here.

 

Earlier today, removed some tools that I'd set on the inner fender that I thought might be causing a short. The diagram indicates that the 3 things on the fuse that blew are the wiper motor, the fuel gauge, and the ignition coil. But for whatever reason, the coil still gets power. Tried cranking the engine with the #1 plug out to see spark and no good. Started thinking I'd be in for a big wiring project.

 

Later today, decided to look through one of my old threads (the Buick 76R). In there, I had to rebuild ALL of the wiring firewall-forward. So I had a bunch of photos wire-by-wire of getting that back together. Noticed the wire between the distributor and coil. That's NOT what's in place on this car. So I looked at generic distributor ignition system wire diagrams, and yes, there's a wire between the distributor and coil. Coil isn't hot continuously, it cycles on/off with each spark. There's a wire in the bundle that goes to the distributor, so I've got that part, but where's the other end? I cut the tape covering the wire harness in that area to open things up. (There's old generator wires I should remove from this anyway, since it's been converted to alternator.) Found the other end. Put that to the coil. Key on, hit the starter, and engine ran almost instantly (on 3 cylinders, since I still had the #1 out). Could see the spark on #1. Not sure what it was running on, as I'd sprayed some starting fluid in there a couple of days ago, but must be some of that & maybe some ancient gas still in the carbs.

 

Pulled the + wire off the coil to kill the engine, and put the #1 plug back in. Started it again, and it runs much smoother on all 4 rather than just 3. Just ran it for a couple of seconds to show that it works, as there's no coolant, but it wouldn't have run much anyway, since I haven't worked out any fuel delivery either.

 

Waiting for replacement clutch / brake master to be delivered, but now I can work on fuel delivery knowing this engine will run.

 

For those wondering about no mention of oil pressure in today's progress - I'd done that earlier. The engine makes oil pressure.

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Worked on getting the cooling system closed up. Pulled the radiator to access the small hose between the head and the water pump outlet. This is a special tiny hose with an accordion center section and a chamfer inside the lower end. Tried pushing it up onto the port on the head, but couldn't get it to move very well. Heated up some water in a coffee cup to near boiling, and dropped the hose in there for a couple of minutes. Then it was much more flexible. It was still a struggle to push it up onto the port on the head, then maneuver it over the water pump port, but it's in.

 

Then was working on the large hose between the pump and the bottom radiator port. There is almost no space at all to get this hose onto the radiator - just a little gap between the back of the radiator and the bottom of the front frame cross member. I fought with that for a while, with only fingertip access to the hose itself, and decided the hose needs to go on the radiator before the radiator goes in. So I pulled the radiator, mounted the hose to the lower port, threaded the upper end of the hose between the steering rack and the frame, and gradually worked the radiator back down into position (pull radiator down a little, pull upper end of hose up a little...).

 

The upper end of the lower hose to the water pump was relatively easy. Then installed the upper hose - also easy. Then the tube to the heater core. This tube is quite a stretch into that port in the longer/lower radiator hose. Put some water on the hose to help. Probably should have added a little soap, but I got it together. Then added a small loop of 1/2" hose (about 18" long) between the heater port on the back of the head to the hard tube along the side of the head, bypassing the heater for now.

 

Added just under 1.5 gallons of coolant. Started engine and let it run until the temp gauge was a little off the stop (~120F). The overflow hose was dripping, and I remembered that I'd bought a replacement radiator cap. So I swapped that on and ran the engine a little more. No major leaks spotted, so cooling is ready for at least some initial drives.

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Got the battery secured. The hold-down hooks from Moss were about 1" too short - need about 5" to the bottom of the threads, ~6" overall length. Modern battery maybe different size from the original. Found some 8" long hooks at the local store and cut about 2" off of them. (photos below)

 

Master cylinder was delivered yesterday, so I got that installed today. Reminded myself of the incorrect order of doing this - needed to put the pedal pushrods into the cylinder before bolting the cylinder to the pedal box, but got that straightened out. Since bleeding the clutch has been the problem, decided to start with that. Decided to back-bleed from the bleed extension hose. Turns out the fitting on the Eezibleed exactly fits into the bleeder extension port, so would be perfect if this works. Put some fluid into the Eezibleed bottle (since the bottle would supply fluid back through the system to the master cylinder), applied the air hose to the tire (for ~20psi pressure), saw fluid leave the bottle a little, then stop. When I let off the air pressure, the fluid jumped back into the bottle. So it won't reverse bleed.

 

Tried to forwards bleed. Added fluid to the master cylinder, drained out the Eezibleed bottle (since it wouldn't need to be the supply), applied the air pressure, pumped the clutch pedal many times, but never saw anything at the bleed hose (from driver's seat, can look under the hood and see the clear hose attached at the bleed extension). Tried this 2 more times, and one time, I thought some fluid left the master and stayed gone, but it's very hard to judge level looking inside the master fill port.

 

Right now, this thing has me defeated. Clutch slave absolutely won't bleed from either end. Will try something like removing the bleed extension and putting the stock bleed fitting back in place, but that requires getting the slave cylinder back off of the transmission, which were a couple of the least-accessible fasteners I've ever had to work with. But I wonder if the fitting for the bleed extension at the slave cylinder is incorrectly blocking the bleed port or something. At least I modified the upper clutch slave bolt before I put it back (cut off about 3/8" of excessively long thread that just gets buried in the bottom of the hole, structurally doing nothing).

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  • 2 months later...

Been a while. Off on other projects around the house, mostly.

 

Tried a couple more times / ways to bleed the clutch - replaced the master cyl and slave cyl, checked the hard line for flow, etc. I'm thinking there's something in the clutch itself that's rusted, so may need to replace the clutch.

 

In order to keep making some progress, I decided to remove the surplus and abandoned wiring from under the hood, specifically on the right side. The original lead to the ignition coil is broken somewhere, and there's no way I can find anything with all the wires covered over and additional unused wires still in place.

 

The car initially came with a generator, but now has an alternator, and I don't think I'm interested in going back. So cut off the electrical tape that was wrapped over the original cloth tape, and cleared off the wires. Removed 2 wires that were part of the generator circuit. Removed 2 other wires - will need to see what these were for, but they had open/exposed ends (potential shorts if they were hot). The car was originally the "square fender", so there was an extra 4-5 feet of headlight leads all wrapped around in there. Shortened 3 of these for the front turn signals / markers, and found that just by disconnecting at existing connectors and reconnecting, I could drop out a couple of feet for the high/low headlights.

 

Also removed the voltage regulator. This caused the work-arounds that allowed the car to get power to the coil to drop out (before starting this wiring rework, the car would start / run), so I'll need to see what should be / needs to be retained from the original regulator connections. But this is progress for today. Unfortunately I didn't have a good "before" picture showing the piled mass of square-fender front light wiring.

 

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  • 6 months later...

Been ignoring this car for a while getting the shop building built. It's about as big as will practically fit with the constraints of this lot. Much more detail here, but here are just a few of the significant steps:

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Wall between front & back yards on the right side of the driveway. Hm - something better than just a yard wall could go here...

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From the backyard - behind that bush is an old hot tub pad. Hm - 80A at 220V power right there...

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Insulated & drywalled - it's built like a house w/o any plumbing. Sure, a sink would have been great, but here on septic, to add another fixture would have cost more than I've got in the Healey...  I did add a mini-split AC after all this was signed off.

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May I make a suggestion. Look online for garage door bumpers. With the jack shaft openers and your door setup, when you close the doors,the door may not move quick enough and the door cables will start to unwind   I know from experience. I hit the door remote and the door didn’t move and the cables unwinded. I had to cut the cables to get the door closed. It took a week before the door company could fix and $400. I looked on line and found the bumpers. They push the door down when the door starts to close. Mike

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  • 1 month later...
  • 2 weeks later...

New year's day, decided to take on the left side rocker. It had some kind of bumpy coating - I guess for protection. Underlying metal was in good shape, except for small hole at the forward end. Sand w/ 80 grit to remove coating, 320 grit to smooth surface, then prime & paint. I know it's not an exact color match - I'm using off-the-shelf paint. This panel is supposed to be body colored.

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Side project - license plate bracket. The license plate mount bracket was rusty, and the decorative chromed frame (pot metal) was corroded, so I made a little aluminum plate to replace both. Also installed the  Sprite trunk script that I'd bought a while back.

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Decided to see if I could do something about the lower rear fender which really didn't look good. While I'm trying my hand with Bondo, I also addressed the pin hole at the forwards end of the rocker. Hm - for all these photos, I didn't get after sanding & before Bondo. There was that step in there to expose some good metal to bond to.

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Left side with the masking paper off. Worked on license plate light. Found out the pot metal light base is the "plinth". Ordered new body-to-plinth gasket, light socket gasket, and lens (which was completely missing). Took 4-5 days of soaking one of the two light socket studs in Evap-o-Rust to remove enough rust to pretty easily unscrew the fastener. I should have taken a before photo for that - it looked like a hopeless ball of rust when I started. Put a little Evap-o-Rust in that corner of the plinth, let it do its thing for a day, pour it out and replace. Only maybe a teaspoon would fit in that corner of the plinth at a time. Just as it says, it didn't react with the pot metal or the rubber seal. Once the light socket was off, could grit blast the plinth to get the old paint off. After a week of dissolving rust, the grit blast was maybe 2 minutes. Primed & painted the plinth.

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During the week, received the additional parts to complete the license light. The replacement rubber between the plinth and the lens housing is much more bulky than what was on there, but I looked at different vendors and they all have the same part. Also looks like this larger part makes a better seal for the lens. Got it all installed with a new wire from the trunk harness, and the lights didn't light. Saw that there was a broken-off contact for the ground side, so ran a wire for that.

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  • 2 weeks later...
  • 3 weeks later...

3 weeks later, car is back home. They diagnosed that the master cylinder I was using was junk, and I'd already had it replaced once as a warranty claim. They said the clutch piston seal was destroying itself in the bore, not making any pressure. They got the other master that Moss sells (the one from U.K.) and got that in there. 

 

Not sure if this is a "first time" or "every time" thing, but they went over the car and documented other items that should be addressed. I held them back from doing any of these at the moment - just get the car back. I suppose you could leave the car there and have them continue to dig into it and replace things, but I've done quite a bit myself, so I'll see what I can cover of their list on my own.

 

One that came up only after they'd got the clutch master replaced & the system bled was that the rear end "shudders". They showed me this by slowly backing the car in front of me - yes, the rear end clearly vibrates or bounces around some. They recommended the rear link bushings. They kindly brought the car back to me yesterday on their trailer, as they didn't want me to get a couple blocks down the road and have an issue. I'm ok with that - saves me driving the car for the first time in traffic, where I have to keep it moving.

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Today, I drove it around my neighborhood a couple of times, and I definitely heard the rear end shudder when backing out of the garage. Going forwards, I guess the links load up and it doesn't vibrate. But I pulled the links out today and will get those bushings replaced. For whatever reason, the rear bushing on the right side link was trashed, and the forward bushing on the left side link was trashed.

 

While out, I have all the hardware in Evap-o-rust, and I'll media blast and repaint the links. Also cleaned the tires with Bleche White. That stuff is amazing. I know these tires are way out of safe age - they don't even have date codes, but they also have essentially all of the tread left. Good enough for getting around the neighborhood while I work out a couple more things.

 

They also identified that the radiator is leaking. When I took the Model A radiator for brazing / leak sealing a couple months ago, the price was SO reasonable, I'll probably pull this radiator and take it to the same place. It looks like the top tank has a slow leak, and the top left attach bracket needs brazing.

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Decided to buy replacement links. For only ~$25/side more, it's a new link, and I wouldn't have to fight pressing out / pressing in the bushings, which I don't have a press or tooling for anyway. Got the limit straps out. Right side first, went pretty easily. Left side, bottom bolt fought the whole way. Straps back in - rear axle really flops around with the links and straps off, but got them back on, not too bad.

 

Links - started with left side. Bottom bolt took a retry to get the flat on the head lined up, but a 5/8" wrench will turn it. Top bolt, wasn't too bad. On to right side - bottom bolt was fighting. Not sure what it was - maybe a burr or something on the threads was sticking in the bushing. Moved to the top bolt - not too bad. Back to bottom bolt - pounded on it with the BFH (4-pound sledge) and got it to where the end of the bolt was even with the axle bracket, but it wouldn't come through. Put the wheels on and drove around the block a couple of times. That did it - moved things around enough that a few more hits with the hammer and the bolt popped through.

 

Just about then, my son got home from school, so I took him around the block a couple of times.

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